Introducing
Your new presentation assistant.
Refine, enhance, and tailor your content, source relevant images, and edit visuals quicker than ever before.
Trending searches
CSX 8888 Runaway Train
May 15. 2001
Where?
The Event: Switching Operation
The Event Continued
Attempts to Stop Train
Reasons and if This Will Ever Happen Again
> unable to board it; speed had increased to 18 mph at mile 4 post
> brake shoes were completely worn to the brake beams
> air brakes were inoperative because of this
* Railroad was prepared to place an additional, fully manned train ahead of the runaway to further slow the train; was not required*
> Crew was instructed to uncouple their single locomotive unit and wait for the runaway train to pass
>2:05 p.m: train passed Dunkirk and Q63615 was ready to enter the main track and pursue the train
> the exact circumstances that combined to cause this event are highly unlikely to happen again
> engineer of Q63615 gradually applied dynamic brake on his train being careful to to break the train apart
> train speed slowed to 11 mph just as it passed Route 31
> Trainmaster Jon Hosfeld ran alongside the unmanned train, climbed aboard and shut down the throttle; train came to a stop
Stanley Yard on the CSXT in Walbridge, OH
(near Toldeo)
> because the dynamic breaking was not selected, shifting the throttle to #8 restores full power to the train instead of delaying the forward movement of the train
> successful in the switch before the train reached it and tried to reboard the train; train was moving at 8 mph
> the train sped up to 12 mph rather than slow down like the engineer thought it would
The Train
> engineer ran to notify yard master of the runaway train
> notified 3 times, but each time, there was no response from the engineer
> noticed he couldn't stop due to the number of cars on the locomotive and the wet conditions
> before passing misaligned switch, he applied the trains independant brakes (applies brakes on locomotive but not on individual cars)