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Transcript

ISHIKAWA DIAGRAM

Network Pwb wire Preparation

Improvement - 4

Improvement - 6

Front grill assembly process

Schedule

FISH BONE CAUSE ANALYSIS

WHY choose this theme?

  • Provided jig
  • Process layout change
  • Improved motion time

Subwoofer packing

Subwoofer supply conveyor

Main Assembly Layout

Tangible result

Improvement - 2

Improvement - 8

Improvement - 10

  • Motion Improvement

Monitoring Of Improvement

Possible causes of low Production

Output and effects (line balancing)

Data Analysis 2 of VIZIO

Possible causes of low Production

Output and effects

Our Team Name & Logo

Subwoofer and sound bar pairing process

Before

After

STANDARDIZATION

After

MACHINE

Improvement - 12

After

MAN

Before

AFTER MAIN ASSEMBLY LAYOUT

Before

After

ITEM

SAVE

COST (RM)

MAIN ASSEMBLY LAYOUT

FINAL

CALCULATION

Insufficient facility

and layout

(Cause sets transferring

& waiting loss)

FINAL

38.06 sec

38.06 X 0.6245 X 450 X 20 X 3 / 60

RM 10,695

Contract worker attendance

turn out insufficient

Eliminate transfer loss

IMPROVE PRODUCTION

YIELD

TOTAL PREPARATION TIME

3.Appearance

4.Packing

RM 7,200

2.Inspection

1.Fix & screw soundbar

TOTAL FINAL ASSEMBLY

2 M/P

2 X RM1200 X 3

New worker training loss

Conveyor too long

28.37 sec

28.37 X 0.6245 X 450 X 20 X 3 / 60

RM 7,972

Front grill pressing machine

TOTAL PACKING

Brainstorming Ideas

PREPARATION

RM 25,867

Grand Total

1) Stick felt to Network Pwb wire one by one.

Push

* Jig design similar to ladder type , as to simplify and reduce hand motion.

Part arrangement

change

Improved 5S

Part arrangement

change

Improved conveyor

PREPARATION

4

6

7

8

12

13

14

15

16

18

4

1

2

3

5

9

10

11

17

19

20

1

2

3

5

1.Existing conveyor line not enough capacity to

cope with the production plan.

2.Production line capacity low.

3.To reduce unnecessary loss on process occured

in production.

4.To improve production & factory efficiency by

strengthen line balancing & facility.

13

14

15

16

17

18

19

B

S

T

Prod. Staff need to pickup Sub Woofer & Sound Bar near to pairing unit place.

E

4

5

3

One P/S is required to place Sub Woofer on working bench. Only 4 unit can be placed.

SAVE

RM25,867

( 3 MONTH )

20

Pull

Eliminate All distractions

32 METER

1

2

1) Make small hanger using Box File Clip to hang HDPE Bag.

Working method impropriate

1) Adjust the positioning Pairing Unit.

2) PS only require to turn & pickup

Sound Bar.

3) Readjust Ac Cord Connector Height

Conveyer design improved will be benchmark for standardization of similar product. ( Plan new project method for new model 2013 )

Plan straight line layout to reduce MP & get optimum quantity.

12

11

10

9

8

7

6

5

4

3

2

1

  • TO INCREASE QUANTITY BY 10%
  • TO REDUCE LOSS TIME

1) HDPE Bag hang on Pipe & Joint for PS to pick & cover Sub Woofer.

2) This bag easily fall down on floor as it's smooth surface.

Design matter cause

material defect

(Button stuck problem)

one time.

2) Input Sub Woofer to Pairing Inspection using new conveyor

3) Same manpower used to support at packing area.

Nature of job distribution

not smooth

Jig is located beside conveyor.

INCREASE PRODUCTION

OUTPUT QUANTITY

BIAQ BETOI!!!

Jig is directly located on the conveyor.

Reduce hand and body motion time.

Reduce push and pull jig process and body

turning motion.

Manpower vs process

not match

Start the Task

3)Using 3 steps Jig by modifying single jig so that 3 wire can be prepared at a time.

6.Hi-pot & vibration test

7.Fix speaker

5.Preparation

8.Transfer next station

2) Make new Single Jig for preparation.

METHOD

MATERIAL

start 2 line-->

Target Achieved

FUTURE PLAN

Line Balancing

Improvement - 3

Speaker unit preparation

Improvement - 5

INTANGIBLE BENEFIT

Group Profile

  • Motion Improvement

Packing Layout

Subwoofer packing

Sound bar packing process

10 meter pairing process

PDCA cycle

Result of improvement

Data Analysis 1 of VIZIO

Monitoring Of Improvement

Possible causes

Improvement - 1

Improvement - 7

Improvement - 9

Improvement - 11

BEFORE PACKING LAYOUT

After

Before

After

AFTER

BEFORE PACKING LAYOUT

Loss time 3

Carton Transfer Slow

Effect The Packing Jobs

Carton transfer slow effect the packing jobs

Monitor progress

Loss time 3

7

AUTO

SEALING M/C

Warehouse

ROLLER CONVEYOR

BELT CONVEYOR

Carton Preparation

8

9

Packing

3

Packing

4

2

6

Wrapping Sound Bar

4

3

Appearance

10

Meter

Pairing

Sound

Bar Unit From Gr.Floor

Mathew (Facilitator)

7

Warehouse

502

Carton

Preparation

Packing

2

386

Packing 1

A

ROLLER CONVEYOR

Part arrangement

change

Improved 5S

How does it occurs?

Production output qty low, sets transferring & waiting loss.

Productivity up 10%.

Set target for the

Improvement item.

5

P

Addition on facility

by Implementation

of the process /

layout change

BELT CONVEYOR

Plan the activity

AUTO

SEALING M/C

9

8

CONVEYOR FOR TRANSFERING SUB WOOFER AFTER PAIRING

Using flip Jig to apply cushion.

Pairing

Packing 4

  • Understanding of Line process group.

  • Upgrade knowledge on Line Balancing.

  • Learn new QC tools.

Packing 3

What is the root cause ?

limitation of the

conveyor system

not suit to the

model.

(Vizio sound bar)

10

1

PAIRING UNIT

Sub Woofer Input

Handling 1

Continue to implement straight

and understanding

INPUT = OUTPUT

to others audio production line.

Nature of job & job distribution

Sound bar unit

Loss time 2

2

Wrapping

Sound Bar

6

After

not even .

Place

Sub Woofer To Table

Place

Sub Woofer To

10 Meter pairing

Appearance

Loss time 1

From Gr.Floor

Possible causes of low Production

Output and effects

Stanble For Pairing

Pairing Unit For Pairing

4

3

KC Ewe

Part arrangement

change

Improved motion

Stick Cushion to Speaker unit inner baffle L & R manually at 3 position.

Ergonomic working method

Improved table height

INCREASE PRODUCTION

QUANTITY THROUGH:

  • Create new conveyor system
  • Process simplification
  • Create fast & speed working

method through facility

improvement

7

AFTER PACKING LAYOUT

Packing 2

Carton Preparation

Packing 1

REDUCE WAITING TIME

1) Packing table height was lower than conveyor

Low Production Quantity

ROLLER CONVEYOR

AUTO SEALING M/C

1) Poor arrangement of Packing material.

2) Effect overall 5'S.

Warehouse

ROLLER CONVEYOR

8

5

9

Where this problem happens?

Audio Production Area

(Vizio sound bar line)

CONVEYOR FOR TRANSFERING SUB WOOFER AFTER PAIRING

Packing 3

Packing 4

ELIMINATE MOTION LOSS

Packing 1

LV Loo-1st speaker

Nikkie - prepare material

Pairing

2

5

Who is responsible

to increase production

output qty?

Prod. Eng’g, Officer,

Technicians, prod. staff

1) Front View of this process shows no facility / improvement done to support prod.

6

13.4

Wrapping Sound Bar

Appearance

4

10 Meter Pairing

3

Sound Bar Unit From Gr.Floor

1

Handling 1

10

1) Make new working table to place packing material in front of P/S (to bring parts/ component nearer to the working area)

Packing 2

Sub Woofer

Input

PRESENT

AC INLET HERE

.

1) Adjust current packing table height to same level of conveyor.

2) Make additional working table to speedup packing process.

1) P/S need to carry & place

Loss time 2

ADD NEW TABLE

after pairing insp.

Job distribution not even

C

  • REDUCE PRODUCTION LOSS
  • PROFIT FOR COMPANY

1

Loss time 1

D

1

Place subwoofer to table stanble for pairing

Place subwoofer to pairing unit

2) Able to support packing if

Do line balancing /

Process change / add

Facility / relayout

CONVEYOR FOR TRANSFERING SUB WOOFER AFTER PAIRING

P/S 10 support at Pairing

Pairing

Insp. (Fully ultilise P/S job)

10

PAIRING

UNIT

1) Rearrange parts as easy for PS to pickup.

SP Foo-line layout

HS Cheng -line layout

Shukery-process study

→ ADD NEW CONVEYOR TO INPUT SUBWOOFER FOR PAIRING

  • For Apr~Jul 12, due to line capacity not enough need to do overtime to cover the balance set

PAIRING

UNIT

Check & Monitoring

the proposal

Why does it happens?

The output qty not tally against the tact time

Chg Present

& ADD 2nd

When it happens?

During production

running.

Sub Woofer Input

.

AC INLET for 2nd Pairing

  • For Aug & Sep 12, need to setup new conveyer system to cater the production plan qty.

Jun 12

Aug 12

Sep 12

Apr 12

May 12

Sep 12

Jul 12

P/S no.10

ELIMINATE TRANSFERING LOSS

After

Input Sub Woofer ,

able to support Pairing Insp

KY Khoo -line layout

Lingam-line balancing

Zaini-data collector

Saniah-animator

Welcome to R-CATS presentation

3 JAN 2013